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Governor's Office of Emergency Services
Hazardous Material Spill Update
CONTROL#: 19-7186 NRC#
NOTIFY DATE/TIME: 11/08/2019 / 1411RECEIVED BY:
OCCURENCE DATE/TIME:
11/08/2019/1330
CITY/OP. AREA:
McKittrick/Kern County

SAN JOAQUIN VALLEY UNIFIED APCD
1.a. PERSON NOTIFYING Cal OES:
AGENCY: Chevron
1.b. PERSON REPORTING SPILL (If different from above):
AGENCY:
SUBSTANCE TYPE:
a. SUBSTANCE:b. QTY:
Amount
Measurec. TYPE:d. OTHER:e. PIPELINEf. VESSEL
>= 300 Tons
1.Water- Produced Type23 Bbl.(s)PETROLEUMNoNo
2. Oil - Crude Type3 Bbl.(s)PETROLEUMNoNo
3. NoNo
Orignal Description:Material discovered pooling on the soil, slow seep from underground, unknown exact source or cause, investigation in progress, RP is making a courtesy notification, RP is handling the containment and clean up.
Update(s): 11/11/2019 05:18:54 PM - : A cumulative total to date is 1,690 barrels, 1,487 barrels of produced water, 203 barrels of crude oil
; 11/12/2019 05:11:46 PM - A culmulative total is 2020 Bbl(s), 1778 Bbl(s) of water and 242 Bbl(s) of oil
; 11/13/2019 04:21:47 PM - RP states: New volumes are, water volume is 1989 bbls, oil volume is 271 bbls, for a total of 2260 bbls.
; 11/14/2019 04:00:20 PM - RP states: updated totals are 2226 bbls of water, 304 bbls of Oil for a total of 2,530 bbls. of material.
; 11/15/2019 04:05:55 PM - Total Amount is 2800 Bbl(s), 2464 Water and 336 Oil
; 11/18/2019 04:25:50 PM - RP states: Water is 3,080 bbls, Oil is 420 bbls, for a total of 3500 bbls of mixed material.
; 11/19/2019 04:00:51 PM - RP states there is an updated amount released of Water 3,318 Barrels, Oil 452 Barrels combined total 3,770 Barrels.
; 11/20/2019 05:02:19 PM - Per RP 3599 Bbls of water and 491 Bbls of oil for a combined total of 4090 Bbls.
; 11/21/2019 06:37:35 PM - Update to the size of the release only.
; 11/22/2019 05:13:30 PM - New totals: 4,030 of Water, 550 of oil, 4580 of total
; 11/25/2019 07:43:58 PM - Called and updated the amount of release to a toal of 5,180 Bbl.(s).
; 11/26/2019 06:41:05 PM - Update to spill size totals only.
; 11/27/2019 05:07:08 PM - RP states Water 5,042 Barrels, Oil is 688 Barrels and total 5,730 Barrels.
; 12/02/2019 04:05:01 PM - QUANTITY UPDATE: Water volume: 5,720 barrels Oil volume: 780 barrels Total volume: 6,500 barrels
; 02/28/2020 03:14:29 PM - Calling from Chevron to report possible seep surface expression per CalGems request, this appears to be a re-activation of this SPILL: 19-7186, release is inside secondary containment, no impacts to waterways or wildlife, no injuries, reactivation of the seep is still flowing at a very slow pace.
; 03/02/2020 09:42:18 AM - Called to update amount and status: A total of 115 Barrels of Crude Oil released, the seep has slowed to a stop.
; 03/02/2020 10:45:19 AM - Per caller, the updated amounts are 14 Bbl(s) of crude oil and 101 Bbls(s) of produced water. Release has slowed to a stop.
; 03/02/2020 04:06:13 PM - Caller updated the amount of release to 150 Bbl(s) of Produced Water , and 20 Bbl.(s) of Crude Oil.
; 03/03/2020 04:56:44 PM - RP states 32 barrels of crude oil and 238 gallons of produced water for a total of 270
; 03/03/2020 05:15:53 PM - RP states 32 barrels of crude oil and 238 barrels of produced water for a total of 270 barrels.
; 03/04/2020 04:11:34 PM - RP advised that the new totals are as follows: 46 barrels of crude oil and 339 barrels of produced water for a total of 385 barrels of fluid released.
; 03/05/2020 04:54:23 PM - RP states produced water updated amount to 444 Barrels; Crude Oil 61 Barrels; total of 505 Barrels of total fluid released.

; 03/06/2020 04:32:52 PM - RP states, 532 Barrels of Produced Water and 73 Barrels of Crude Oil; 605 Barrels of total fluid released.
; 03/06/2020 05:10:28 PM - 605 bbls of fluid total, 532 bbls of produced waater and 73 bbls of crude oil
; 03/09/2020 04:57:57 PM - Caller updated the amount of release to 118 Bbl(s) of Crude Oil and 867 Bbl(s) of Produced Water for a total release of 985 Bbl(s).
; 03/10/2020 04:52:38 PM - Per the caller the produced water volume is 1,021 bbls and the crude oil volume 139 bbls for a total 1,160 bbls
; 03/11/2020 05:23:47 PM - Caller states 1,162 Barrels of Produce Water and 158 Barrels of Crude Oil; for a total of 1,320 barrels of fluid released.
; 03/12/2020 04:55:08 PM - Caller states 1,346 barrels of Produce Water and 184 barrels of Crude Oil; for a total amount of 1,530 barrels of fluid released.
; 03/13/2020 04:45:15 PM - Caller states 1,530 Bbl(s) of produced water and 217 Bbl(s) of Crude Oil for a Total 1,810 Bbl(s) of material released.
; 03/16/2020 03:58:27 PM - Called to update amount: The cumulative total at this time is 2,530 barrels of material (2,226 Barrels of Produced Water, 304 Barrels of Crude Oil).
; 03/17/2020 04:36:56 PM - Caller states, 2402 Barrels of Produce Water, and 328 Barrels of Crude Oil; total of 2730 Barrels of total fluid released.
; 03/18/2020 03:59:03 PM - Per the caller the produced water volume is 2,605 bbls and the crude oil volume is 355 bbls for a total combined volume of 2,960 bbls
; 03/19/2020 05:05:22 PM - Caller states updated amount of produced water is 2878 barrels, crude oil updated amount is 392 barrels. Total fluid amount is 3270 barrels.
; 03/20/2020 04:40:58 PM - Caller states the produced water amount is now 3098 barrels, the crude oil volulme is 422 barrels, for a total of 3,520 barrels total fluid.
; 03/23/2020 05:35:32 PM - Caller states at CALGEM's request RP is reporting volumes released from Guage Setting #5 02/28/20 reativation event after 03/20/20 is under a new spill report Cal OES 20-1649. Flow volumes entered for 02/28/20 through 03/20/20 are from a reactivation from of the 19-7186 event. Per CALGEM's request a new report was created on 03/23/20 to record the volume assoiciated with the event beginning on 03/21/20. The report #20-1649 reports the volumes from 03/21/20 forward.

PERSON NOTIFYING Cal OES OF SPILL UPDATE:
NAME:
AGENCY:
PHONE#:
Ext:
PAG/CELL:
UPDATE QUANTITY
Amount
    Measure
1.
    Bbl.(s)
2.
3.
4.

UPDATE KNOWN IMPACT:




UPDATE CAUSE:

SITUATION UPDATE:
Caller states at CALGEM's request RP is reporting volumes released from Guage Setting #5 02/28/20 reativation event after 03/20/20 is under a new spill report Cal OES 20-1649. Flow volumes entered for 02/28/20 through 03/20/20 are from a reactivation from of the 19-7186 event. Per CALGEM's request a new report was created on 03/23/20 to record the volume assoiciated with the event beginning on 03/21/20. The report #20-1649 reports the volumes from 03/21/20 forward.
Link to Spill Report:
FAX NOTIFICATION LIST:
AA/CUPA, DTSC, RWQCB, US EPA, USFWS, DOG, Cal OES HAZMATUNIT, Cal OES PLANS UNIT, Cal OES REG, SFM, Co/WP, Co/Hlth, Co/E-Hlth DOG
ADMINISTERING AGENCY:Kern Co. Environmental Health Services Department
SECONDARY AGENCY:
ADDITIONAL COUNTIES:
ADDITIONAL ADMIN. AGENCY:
DOG Unit:
OTHER NOTIFIED:DOG
RWQCB Unit:5C
Cal OES Region:

CONFIRMATION REQUEST:

Please confirm receipt by reply email or phone 916-845-8911.



FAX NOTIFICATION LIST:


ADMINISTERING AGENCY:


ADDITIONAL ADMIN. AGENCY:


SECONDARY AGENCY:


ADDITIONAL COUNTIES:


Cal GEM:


RWQCB Unit:


Cal OES Reg.


Created by: Warning Center on: 03/23/2020 05:35:32 PM Last Modified by: Warning Center on: 03/23/2020 05:42:34 PM
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